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The
arrival of the 725
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REBIRTH
OF A 725
by John Tilley
Following what
appears to be a natural progression from a Locomobile, I looked
around for a Stanley to restore, to find the only available project
was a rather daunting one of a chassis and boxes of bits belonging
to Sprague register page 46.
I made a visit
to the current incumbent David King and viewed the various boxes
and crates, fairly evenly spread in garages around Melksham, and
then quite reasonably concluded that it was a most unattractive
proposition. However, after one or two other disappointing leads,
it appeared to be the only proposition, so a trip was made with
pickup and Locomobile trailer to collect the ton of what I hoped
would add up to an original car.
The only item
to have had any attention since the dismantled car was shipped from
Oregon in 1972 was the chassis which had been cleaned and primed
by importer Alan Griffith. This was in good original condition as
were both axles, but hubs and wheels needed rather more effort.
The engine block
was excellent, virtually unmarked. The valve spindles and guides
were replaced, as were the cross head guides. Surprisingly, one
cylinder head plug has such loose threads that I feared it would
blow out, so I made a new one. The boiler included in the "kit"
had around 1500 steel fire tubes about 5/16 O.D which were obviously
not original Stanley. Judging by the corroded state of the tube
ends, these were not even worth pressure testing, so a new shell
was collected from John Goold. I then spent weeks agonising over,
but only three evenings actual expanding, the seven hundred and
fifty 1/2" O.D, 1 8g copper fire tubes. My agonising was based on
engineering knowledge that copper rapidly loses its mechanical properties
above 2OOdeg.C. and we happily run the boiler at 26Odeg.C plus superheat
at almost unheard of pressures! I had grave doubts on the security
of the expand ends, and did in fact firstly roller expand the tubes,
to give a parallel expansion, before "bashing" in, the ferrules.
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John
in his Stanley pickup and below as the car was as it first
steamed out of the garage

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I have since
been appraised of the fact, by a metallurgist friend, that if one
takes some copper in its annealed state, then its properties remain
little changed up to 4OOdeg.C or so, but 1 8g annealed copper fire
tubes at 550 psi? What ever my pre-conceptions, the boiler along
with dozens of others of similar construction performs just fine!
Most of the
original burner and pilot was re-housed in a new casing, and I discarded
the original vaporiser, which included a smoke hood 'pre vaporiser'
in favour of a straight tube 'ottoway' type.
The automatics
all scrubbed up well and although the controls included a three
tube water level device, (which I have plumbed in, but not yet commissioned)
I've added a Klinger type sight glass nestled between the foot boards.
A valuable part of the 'kit' to my mind at least, is the original
firewall board, complete with guages and original somewhat crazed
paint, now carefully preserved.
Although against
my principles of 'spend the winter making it and the summer using
it', I accepted this as a two winter project, so on May 1st (my
symbolic opening of workshop doors) the Stanley appeared on the
drive in chassis form with me sitting on a kitchen chair, creeping
along on 120 psi compressed air fed into a blow down.
The next winter
began with extensive pipework, following the Stanley 'knitting pattern'
piping diagram, complete with a few deliberate mistakes to keep
me awake! I had decided not to copy a 5 seater body, which it may
well, but not certainly had had, but came up with an English body
as though it was an imported chassis. I had vision of a two seat
pickup style, but the Stanley 'delivery wagon' illustration shows
something rather more basic than comfortable. The design eventually
to emerge was a part copy of the Stanley five seat up to the rear
of the front seats, then add a timber pick up back. This all took
shape pretty much to program, with a contribution from an American
ash tree and a local (Hinkley) panel beater and upholsterer. I did
notice that the car assembly sequence would mean that, if any chassis
work was later found wanting it would involve painful dismantling
of the whole body, so a trial steaming was arranged, with me on
the same kitchen chair, but engulfed in steam (which fortunately
masked my terrified countenance) before final assembly began.
I must say
it did perform rather well, or at least it didn't explode, or catch
fire - much!
A bit more work,
a few coats of paint, and May lst(ish) out came SV 8661 an accredited
and street legal (ha!) Stanley 735 pick up truck. A small celebration
steam car meet was arranged to introduce 'Stanley' some of his friends,
and we had a short trip with seven SCC diehards as cargoe.
I subsequently
fitted a canvas 'tilt' and we have made a weekend trip, over nighting
in reasonable comfort in the back. Have I the first steam powered
camper? I've added a number of 'ideas' to improve comfort, safety
and reliability that are worthy or note.
- A standard 'mini' alternator in place of the axle driven dynamo,
geared up 2.5:1 with a timing belt drive. This cuts in at 8mph
and provides adequate battery power.
- An under floor lamp to illuminate the Klinger guage, operated
by a foot switch.
- Oil tolerant brake linings, which are as used on crane brakes
and really do perform well. |
- A Les Nelson water pump discharges pressure guage, it really
does tell you instantly if you are pumping, by-passing or have
run out of water!.
- A three way 'shoe valve' on the condenser to water tank line,
this allows me either to return the condensate to the tank,
or dump it. My inclination is only to re-use condensate when
circumstances demand (ie no ready water on route anticipated),
to reduce as much as possible oil return to the boiler.
- A smoke hood secondary feed water heater, from 3/8" s.s pipe,
to compensate for the A smoke hood secondary feed water heater,
from 3/8" s.s pipe, to compensate for the non-condensing cold
water tank syndrome.
- A flue stack steam blower, just/pipe with a 1/16 nozzle fitted
in the top bend. This does 'lift off any burnbacks at the nozzles.
- Make a 'short' steering drop arm from 8" to 5" to reduce the
incredible steering effort, due in part to the 600 section tyres.
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